Final Performance Test Design

Below is the design that was used for the final Performance Test of the AEV project. One difference between this design and the design used for the previous performance tests was that the Arduino was moved to the bottom near the back of the AEV and the battery was placed in the front section. This change was made because the Arduino could not be close to the magnet on the front. Also, the propellers were switched to be facing the opposite direction. The group decided to do this in order for the AEV to use less energy/power when traveling backwards, pulling the caboose.