3/7 Test

Purpose of Test: Complete Performance Test 3

Observers: Tom, Shyon, Dean, and Meghan

1st Run (3:23, Course B): Robot completed Performance Test 3 without failure.

2nd Run (3:24, Course B): Bump switch broke off and robot did not complete course.

Changed: Hot glued bump switch back on initial location.

3rd Run (3:30, Course G): Robot’s turns were inconsistent, axles kept getting caught on the course and turning robot at weird, incorrect angles.

Changed: Line up robot against wall more to try and be more consistent.

4th Run (3:35, Course H): Robot consistently inconsistent, drifting to the left when it approaches the garage.

Changed: Account for the leftward drifting and compensate for it.

5th Run (3:41, Course E): Still inconsistent when moving towards garage.

Changed: Tried to secure bump switches more.

6th Run (3:50, Course B): After a few inconsistent attempts, the robot failed some and succeeded during others. The team decided to do an Official Run™ and succeeded on the first attempt.

Source Code

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